
This locomotive was built in 1891 by Manning and Wardle & Co and supplied new to Logan & Hemingway. The locomotive has two inside 12 in cylinders, 3 ft diameter wheels and weighs 19 tons 4 cwt.
Logan & Hemingwaywere a firm of engineering contractors who during the latter half of the 19th century and the first third of the 20th century worked mainly on railway (and allied) constructions. They were steady customers of Manning Wardle, working the engines hard, selling the older locomotives when business waned and re-stocking with new as contracts required.
The locomotive was given the number 30 and was used to help build the Manchester, Sheffield & Lincolnshire Railway (later to be the Great Central Railway) and was noted on the excavation of the Nottingham GCR/GNR joint station site (eventually named Nottingham Victoria). A slack period followed completion of the GCR, and thinning out their fleet saw the locomotive renumbered as 10. It is then known to have worked on the Wath Concentration Sidings (1905-07) and the Doncaster Avoiding Line (1908-09) in Yorkshire (both contracts for the GCR), then (still on GCR contracts) in Lincolnshire during 1910-15, first at Frodingham Viaduct in-filling, then at the Keadby Deviation Line construction.
No. 10 was next used at the Thoresby Colliery (Nottinghamshire) branch line construction in 1925-26, the Crofton Tunnel Widening at Barnt Green (Worcestershire) for the LMS in 1926-27, then back to Thoresby Colliery in August 1927 for a couple of months before working on the Hattersley Widening between Mottram and Godley Junction (east of Manchester) for the LNER. In 1930 No. 10 went south to the Wiltshire/Somerset border for its last railway contract, the GWR Westbury and Frome Cut-Offs.
In 1935 Logan & Hemingway went into liquidation and the locomotive was sold to the Cranford Ironstone Company of Kettering (Northamptonshire) where it received the nameplates Sir Berkeley from a scrapped Manning Wardle engine owned by the Midland Ironstone Company at Crosby (near Scunthorpe). To the Cranford workforce however, it was always known as “Paddy Logan”.
Sir Berkeley’s work at Cranford consisted of hauling four (six with banking assistance) loaded ore wagons from the quarry face to the storage sidings, or from the storage sidings up an incline to the LMS interchange sidings. Between 1943 and 1947 it was loaned to the Pilton Quarry in Rutland where a steep incline down to a dead-end siding at the quarry face exposed the limitations of Manning Wardle’s handbrake, even though fitted to act on all wheels in accordance with Logan & Hemingway’s standard requirements for all their Manning Wardle engines. During the early 1950s Sir Berkeley underwent a complete renovation, during which the original weatherboard was replaced by an open-backed cab, a Wakefield mechanical lubricator was fitted, a new sheet-steel sandbox was fitted on the right hand side and the original wooden dumb-buffers were removed. The motion was completely dismantled, bearing surfaces were re-metalled, pistons re-ringed and when the whole was re-assembled the valve events were re-timed for optimum efficiency.
At the end of 1957 Cranford Ironstone acquired a Hudswell Clarke 0-6-0ST to replace Sir Berkeley which then became redundant, except for occasional duties as a stand-in for any engine that was undergoing a boiler washout, or some other maintenance operation.
In 1959 it was transferred to the associated Byfield Quarries and worked alongside another Manning Wardle locomovite (MW 1235 a class K of 1893). MW 1235 was subsequently was cannibalised to provide spares for Sir Berkeley.
In 1960 Sir Berkeley was yet again made redundant and with its days as a commercially useful engine over it languished in a siding for a couple of years before being formally retired in 1963.
The locomotive was bought in 1964 by Roger Crombleholme, just in time to save it from being scrapped, and was moved to the Worth Valley Railway in 1965 where its original weatherboard was refitted, having been discovered at Cranford. Restored to service it took part in the BBC Television production of The Railway Children.
After expiry of its boiler certificate the Vintage Carriages Trust bought the engine and firstly kept it as a static exhibit but in the course of time restoration to working order took place. Since then Sir Berkeley has travelled extensively within this country and abroad, having been in use at British Steel Scunthorpe, the East Anglian Railway Museum, the Dutch National Railway Museum and the Middleton Railway at Leeds, which is its present location.
The ten year boiler certificate expired in 2001 and a new boiler was made in 2006 byIsrael Newton of Bradford with the assistance of a grant of £50,000 from the Heritage Lottery Fund.
Sir Berkeley returned to service at the Middleton Railway on Saturday April 14th 2007.
The locomotive remains on loan from the Vintage Carriage Trust to the Middleton Railway where it is operational.
This locomotive was built in 1891 by Manning and Wardle & Co and supplied new to Logan & Hemingway. The locomotive has two inside 12 in cylinders, 3 ft diameter wheels and weighs 19 tons 4 cwt.
Logan & Hemingwaywere a firm of engineering contractors who during the latter half of the 19th century and the first third of the 20th century worked mainly on railway (and allied) constructions. They were steady customers of Manning Wardle, working the engines hard, selling the older locomotives when business waned and re-stocking with new as contracts required.
The locomotive was given the number 30 and was used to help build the Manchester, Sheffield & Lincolnshire Railway (later to be the Great Central Railway) and was noted on the excavation of the Nottingham GCR/GNR joint station site (eventually named Nottingham Victoria). A slack period followed completion of the GCR, and thinning out their fleet saw the locomotive renumbered as 10. It is then known to have worked on the Wath Concentration Sidings (1905-07) and the Doncaster Avoiding Line (1908-09) in Yorkshire (both contracts for the GCR), then (still on GCR contracts) in Lincolnshire during 1910-15, first at Frodingham Viaduct in-filling, then at the Keadby Deviation Line construction.
No. 10 was next used at the Thoresby Colliery (Nottinghamshire) branch line construction in 1925-26, the Crofton Tunnel Widening at Barnt Green (Worcestershire) for the LMS in 1926-27, then back to Thoresby Colliery in August 1927 for a couple of months before working on the Hattersley Widening between Mottram and Godley Junction (east of Manchester) for the LNER. In 1930 No. 10 went south to the Wiltshire/Somerset border for its last railway contract, the GWR Westbury and Frome Cut-Offs.
In 1935 Logan & Hemingway went into liquidation and the locomotive was sold to the Cranford Ironstone Company of Kettering (Northamptonshire) where it received the nameplates Sir Berkeley from a scrapped Manning Wardle engine owned by the Midland Ironstone Company at Crosby (near Scunthorpe). To the Cranford workforce however, it was always known as “Paddy Logan”.
Sir Berkeley’s work at Cranford consisted of hauling four (six with banking assistance) loaded ore wagons from the quarry face to the storage sidings, or from the storage sidings up an incline to the LMS interchange sidings. Between 1943 and 1947 it was loaned to the Pilton Quarry in Rutland where a steep incline down to a dead-end siding at the quarry face exposed the limitations of Manning Wardle’s handbrake, even though fitted to act on all wheels in accordance with Logan & Hemingway’s standard requirements for all their Manning Wardle engines. During the early 1950s Sir Berkeley underwent a complete renovation, during which the original weatherboard was replaced by an open-backed cab, a Wakefield mechanical lubricator was fitted, a new sheet-steel sandbox was fitted on the right hand side and the original wooden dumb-buffers were removed. The motion was completely dismantled, bearing surfaces were re-metalled, pistons re-ringed and when the whole was re-assembled the valve events were re-timed for optimum efficiency.
At the end of 1957 Cranford Ironstone acquired a Hudswell Clarke 0-6-0ST to replace Sir Berkeley which then became redundant, except for occasional duties as a stand-in for any engine that was undergoing a boiler washout, or some other maintenance operation.
In 1959 it was transferred to the associated Byfield Quarries and worked alongside another Manning Wardle locomovite (MW 1235 a class K of 1893). MW 1235 was subsequently was cannibalised to provide spares for Sir Berkeley.
In 1960 Sir Berkeley was yet again made redundant and with its days as a commercially useful engine over it languished in a siding for a couple of years before being formally retired in 1963.
The locomotive was bought in 1964 by Roger Crombleholme, just in time to save it from being scrapped, and was moved to the Worth Valley Railway in 1965 where its original weatherboard was refitted, having been discovered at Cranford. Restored to service it took part in the BBC Television production of The Railway Children.
After expiry of its boiler certificate the Vintage Carriages Trust bought the engine and firstly kept it as a static exhibit but in the course of time restoration to working order took place. Since then Sir Berkeley has travelled extensively within this country and abroad, having been in use at British Steel Scunthorpe, the East Anglian Railway Museum, the Dutch National Railway Museum and the Middleton Railway at Leeds, which is its present location.
The ten year boiler certificate expired in 2001 and a new boiler was made in 2006 byIsrael Newton of Bradford with the assistance of a grant of £50,000 from the Heritage Lottery Fund.
Sir Berkeley returned to service at the Middleton Railway on Saturday April 14th 2007.
The locomotive remains on loan from the Vintage Carriage Trust to the Middleton Railway where was operational for some time.
In August 2019 it was reported that the overhaul of the locomotive at the Middleton Railway was making good progress towards a return to steam. In January 2020 the Middleton Railway said that the plan was that the overhaul of the locomotive would be completed with the aim of having it back in traffic for the start of the 2021 season.
In May 2022 it was noted that the boiler had passed its boiler test and had been lifted back onto the frames at the Middleton Railway during that month.
The locomotive was returned to steam in November 2022 but did not enter traffic again until April 2023 as planned.






